Since completion of my vertical Domestic engine, I had not been able to get it to run properly and consistently. The problem was due to two things, both having to do with the fuel flow.
It's a poor design, at best, with fuel flowing into the mixer by gravity, and even the difference between a full tank of fuel and a near empty tank causes a difference in the fuel flow to the mixer. The real problem, though, was in the fact that there was no fine adjustment for the fuel mixture, with the mixing screw needle made according to the blueprint.
The first picture shows the mixing screw made to spec. This simply made it nearly impossible to have any real adjustment of fuel flow, as this large tapered needle seated in a number 60 drilled hole. I have tried turning thinner needles with a finer taper on the lathe, but they never come out right, or they bend before I'm finished.
I finally got the idea from one of my old wind-up phonographs, to cut the end off the mixing screw and solder an old phonograph needle into the end of it. It has the perfect fine-tapered end that I needed, and the engine has now been able to be fine-tuned to run perfectly.
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